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We've finally found and fixed the communication bug that was causing the flight controller crash and wonky gimbal pitch control in 3.7-dev. Tridge found the issue in i2c that was causing an interrupt storm, eventually saturating 100% CPU and crashing it. The same i2c interrupt storm was causing packet loss from the gimbal, screwing with the gimbal EKF. The communication bug has been fixed, and now both of those problems are resolved. Those fixes went into master yesterday, and everything is now working great! I put the latest ArduCopter 3.7-dev for Solo up in Solex and SidePilot, dated 8/25/2019.
This constitutes all the remaining bugs in 3.7-dev related to the Solo safely and reliably flying on master. So when the next major ArduCopter stable release comes out (it will be ArduCopter v4.0.0), it will be 100% solo compatible for all solos.
This constitutes all the remaining bugs in 3.7-dev related to the Solo safely and reliably flying on master. So when the next major ArduCopter stable release comes out (it will be ArduCopter v4.0.0), it will be 100% solo compatible for all solos.